• Sole mechanical designer/engineer utilizing CNC, MJF, waterjet, sheet metal, 3D printed silicone, and other processes to accelerate development time during challenging logistic constraints.
  • Exceeded dock reliability margins with 99% success across thousands of tests.
  • Planned and executed a tolerance study of the robot’s positioning biases to reduce package size in the dimension of highest precision.
  • Designed highly integrated indexing and connector enclosures under tight volume and mass budgets.
  • Created custom high-cycle, self-cleaning electrical connector assemblies and actuation mechanisms to meet IP54 ingress protection and safely cover hot contacts.
  • Collaborated with software engineers to separate changes worth solving in the behavior versus the dock to minimize project timeline.